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Third time not lucky

Having failed twice to get the engine running – at the expense of a weekend of time and a thousand miles of driving (return trip distance) each time, I was keen to succeed this trip and had prepared better (though not exhaustively) for anticipated problems. Since the second trip had determined that the engine was not even turning over (having at least done that on the first trip) I came with some new toys, specifically a 40″ breaker bar with a 1″ drive and some corresponding sockets:

Happily, turning the engine over by hand with the breaker bar was very easy, ruling out mechanical issues (which had been a slight concern only because I had been cranking it with cooling water hooked up previously). Having ruled out physical seizure of the engine, the next thing to investigate was the electrical connection between the battery and the starter motor, for which I also came prepared with a brand new Perko battery selector – the heaviest duty 2 way selector they make.

At this point I opened a new can of worms – not a surprise inasmuch as with boats one often stumbles into decisions by prior owners or builders that one disagrees with. I found the original Perko switch (just a simple switch, not a selector) was damaged inside – and rated for far fewer amps than I understand this starter to draw (up to 600A). Note the melted plastic on the upper terminal in the below picture and the amp ratings – 250A continuous and 350A intermittent.

Original damaged Perko switch, insufficient amperage rating for starter

It often seems to be the case that people economize with such things, but in my view this is very much a false economy. While clearly the vessel was running with this equipment historically (ie it technically worked, at least in ideal conditions) – to melt out the battery terminal and Perko switch well before the starter motor even became warm to the touch tells me that there really wasn’t enough safety factor here. You want to be confident your engine starting system will give you it’s very best in a critical situation. It’s really not worth saving $150 on the cheaper switch here if it may cost the vessel or the lives of those aboard.

Note below the replacement Perko switch, rated to 850A intermittent (which should provide reasonable safety margin versus the 600A the starter can draw). This one is intended to also allow me a backup starting battery – or the option to start from two batteries at once. The original set up has no such safety provision – although there is a space for a second battery in the engine room, it is set up to power the anchor windlass (for which I intend to install a dedicated battery much nearer to the bow).

Newer, bettery, chunkier – heaviest duty Perko selector switch available

At this point I ran into another issue, which is that the terminals on the new Perko switch are bigger than on the old (to accommodate the higher current flow). At this point I calculated voltage drop for the existing 2/0 AWG battery cables and determined that with the existing cabling I can expect minimum drop around ~10% improving to ~5% if I upsize to 4/0 AWG. Since these are best case estimates, I also regard the cabling as lacking sufficient safety margin, even in the starter motor scenario (where relatively more voltage drop can be tolerated).

I had not originally anticipated weakness in the starting system as the vessel was professionally built (by Topper Hermanson in Jacksonville FL) and my assumption was that the critical systems would be accordingly robust. However, it is rather common one runs into these cans of worms with a newly purchased vessel and opinions as to safety factor do vary.

Being unable to replace the cabling and terminals on the spot, I decided to bypass the original Perko by bolting the existing cables together for the purposes of continuing to troubleshoot (with a generous helping of insulation tape to safeguard against shorting the battery, as the whole system passes through a common ground that is also bonded to the metal hull).

From here I proceed to successfully crank the engine with the starter with pauses for the system to cool and longer breaks to recharge the starting battery. Besides purging as much air as possible via the injector bleed valve I cracked and bled the injectors themselves.

Since the engine still steadfastly refused to start I even tried applying a little ether via the air intake (which I’m not generally a fan of). The engine would fire on ether but at no time sounded like it was in danger of doing so on diesel.

Observing that the hand priming pump loses prime over time and after cranking, and that the racor filter is draining back into the fuel tank I believe it is most likely that the engine is failing to start owing to a leak somewhere in the fuel system. Since the system is all suction based, there is no conveniently dripping diesel to help trace this and I had not prepared to work through this issue on this trip.

Consequently this can be considered progress; and certainly I’m learning more about my engine even if it is not yet running. Next trip I will take replacement fuel filters and a means to help trace leaks in the system – and start another project in parallel as it’s a long way to drive to fail to start an engine.

If at first you do not succeed, fail again

The last time, the engine was cranking with a starter battery hooked up – right up to when the battery terminal melted and the negative lead detached.

Consequently this time I expected to hook up a new battery, bleed the engine to the injectors and most likely have it running fairly easily after that.

So I installed the new battery:

Another day, another 8D

I hooked up my water supply to stop the raw water pump impeller from burning out:

It’s not much more than a toilet plunger with a hose connected to it.

I cracked an injector and primed the diesel system until diesel came out of it (which I wasn’t sure I’d be able to do without the engine turning, as that’s on the high pressure side, but it seemed to work fine).

Finally, I went to the helm and turned the ignition key for the moment of truth…

… and nothing happened.

Most likely I damaged something else last time I tried, but I didn’t bring either the tools or the time on this trip to do anything more with the engine this time.

Retreat, re-plan and revisit…

At least it didn’t explode

The first objective for Tenacious is to get the engine running. One of the many lessons learned from Guanahani was to focus on core systems first and not branch out into too many different projects simultaneously.

Since Tenacious came with no batteries at all I needed at least 1 starting battery for the engine. An 8D battery is sufficient for this.

First one must install the battery. Simple enough – except that this 8D battery weighs 130lbs and must be carried up these steps, lugged through the vessel, man-handled into position in the engine room and securely fastened to the correct terminals.

With my never having run the engine before, prudence also dictates checking the fuel lines and valves, the coolant, the oil, the air filter and the control system.

Eventually (with the appropriate amount of swearing) the battery was installed by the engine and hooked up. So far so good:

8D battery installed in design location in engine room corner

Having checked over the engine, I tried operating the starter. The starter cranked the engine, but there were no sounds of it trying to fire. After a few tries, I realized I hadn’t bled the air from the fuel lines and looked up how to do this on this engine.

Having bled it as indicated (with a priming pump and a valve that opens until fuel is dumped out into the bilge), I tried cranking the engine again. It still did not want to start, but I figured it hadn’t run for a long while and there was likely air in the system so I kept trying, with suitable delays for the starter and cabling to cool down (or so I thought).

After a number of additional attempts I went below to inspect the relevant components in the engine room. The starter and cables were warm but not ridiculously hot. However, I noticed that the cable on the negative post of the battery was loose – on closer examination the terminal had failed (nearly completely; yet the engine had still cranked without obvious complaint the previous try).

Bad battery or user error?

This was the end of any attempts to start the boat, and rather frustrating. As always these things are learning experiences, and I learned:

  • Terminals on these batteries are lead, presumably to ensure they melt easily, I assume to protect everything else (and reduce the risk of battery heat/explosion)
  • Properly speaking it seems they should be tightened to torque, and checked periodically. None of the material listing the battery on Napa’s website mentions this however.
  • On a sea going boat, this mode of failure is a liability. This type of top post is therefore an unsafe choice as one might need to aggressively crank the engine to get out of trouble in some circumstances. I need a top post connection with more surface area and less chance of failure.

I believe heat built up in the terminal and gradually softened it until the lead was able to start pulling free. I decided to attempt to recast the terminal in lead at some later date and explore the possibility the battery could be used to power the anchor windlass instead (given these batteries are disturbingly expensive). The goal of starting the engine was not achieved, but it was at least confirmed that it could be turned by the starter with a suitable battery attached.

Battery acid on aluminium would react rather vigourously, so I am asking myself if I can construct some sort of secondary containment for the batteries just in case any should ever leak. This time at least, it didn’t explode.